Car hit the dyno and after the 9:1 compression change we hit 380/250 at the wheels however there is speculation the dyno wasn't reading correctly but still sitting AT LEAST 100WHP away from the target 500WHP goal.
Good news is the full Ti rebuilt head looks to be stable to 11K YUP 11,000 RPMs. Guess the handle punchit8k needs to change -_-
After the dyno we ran into some overheating issues that are EXTREMELY weird. Take the car out for a beat run no problem car holds nice and cold. Park it and on the next startup it will overheat. Burp the cooling system and it runs fine again.
Replace radiator with a koyo radiator, new cap, lines. Still doing the same thing. What we found was one of the coolant lines under 30psi had a SMALL SMALL leak. Now the coolant system will never hit 30psi BUT the theory is that on cool down the car was sucking in a small bit of air and these damn cars are temperamental. Anyways won't know if it's fixed 100% until the spring.
Here are some videos/photos of updates:
11K RPM dyno pull, we backed down to 9500 RPM redline due to the supercharger overspinning. Won't be an issue down the road
Strapped down:

Js racing Dry carbon canards installed with nutserts yea I know the whole car needs to be painted when it's done...


RX7 Side splitters installed finally:

In the spring we're looking at Intake manifold (matched 74mm TB), 3" exhaust, larger intake and possibly changing up some of the body panels.











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